exelbaradin
New Member
- Joined
- Dec 28, 2021
- Messages
- 8
- Reaction score
- 24
so the history behind this car was a purchase out of necessity. our previous car was a little corolla and it got hit and totaled. so we got this car quickly to get back on the road.
we got it with already higher in its mileage life, roughly 195,*** on it and a check engine light for an oxygen sensor heater circuit that had come up with the previous owner when someone stole a cat off the thing and i had fun figuring out what the issue was with that... when they stole the cat they cut the wire with the harness and i could not find a liberty the same year in the junkyard the same year (i guess theres different connectors at the end and different wire colors).
Right away I got to repairing the wiring down there and once that got sorted I started down the list of maintenance that was long overdue and needed
Started with a trans service. The fluid was new but I wasn’t sure if they had put atf +4 in it so I did it
I also did a diff service, and oil pan gasket.
I wanted to eliminate all the leaks I could.
I don’t remember exact where in the timeline it was I just know it was early on that we learned the heater core was leaking… so I pulled the dash and replaced the heater core and ran the wiring for a rear view camera while we were at it.
Few weeks later took the front grill off and had a buddy polish the headlights and fog lights for me
At this point I had starting doing all the over suspension work as well
New ball joints
New bushings in the lower control arms
New upper control arms and new rear upper control arm all from moog
I also started looking into a small lift for it and went with the rusty off-road strut spacer and poly block
It went in great but about after a week or so I had this annoying squeaking in the front which I originally thought was the coil spring rubbing on the frame and I had just got the new upper control arms so I didn’t want to go buy jba ones
So I decided to take it all apart again
And this is what I found
The washer from the strut assembly was slightly rubbing onto the lift spacer….. what I get for being cheap
But I took a grinder to the washer and solved my problem.
So at this point I had fixed all the oil leaks, done all my maintenance I was ready for do other little mods and get some new tires for the lift
Installed a new steering wheel, xtrons android head unit (I didn’t want to change the OEM look)
At this point the flaws of the worn engine and trans were starting to show themselves I had an oil consumption issue. No leaks, new pcv valve and every 1500 miles was down a quart of oil
And I had to start topping off the coolant every month.
No overheating, i had already done dealt with a garden hose effect with the cooling system
Heater core was first then the radiator and coolant hoses with a new thermostat, then the water pump started leaking. So I knew I was at the point of cut my losses and get rid of it or ride it out as long as it last and fix it. We decided we liked it and to ride it out want fix it.
So we kept nursing it along and the trans started to develop a noise that i can only describe as a mosquito buzz.
I didn’t a bunch of reading and what I ended up doing was removing the cooler lines bypassing the cooler (just for the test) and the noise went away..
we got it with already higher in its mileage life, roughly 195,*** on it and a check engine light for an oxygen sensor heater circuit that had come up with the previous owner when someone stole a cat off the thing and i had fun figuring out what the issue was with that... when they stole the cat they cut the wire with the harness and i could not find a liberty the same year in the junkyard the same year (i guess theres different connectors at the end and different wire colors).
You must be registered for see images attach
Right away I got to repairing the wiring down there and once that got sorted I started down the list of maintenance that was long overdue and needed
Started with a trans service. The fluid was new but I wasn’t sure if they had put atf +4 in it so I did it
You must be registered for see images attach
I also did a diff service, and oil pan gasket.
I wanted to eliminate all the leaks I could.
I don’t remember exact where in the timeline it was I just know it was early on that we learned the heater core was leaking… so I pulled the dash and replaced the heater core and ran the wiring for a rear view camera while we were at it.
Few weeks later took the front grill off and had a buddy polish the headlights and fog lights for me
You must be registered for see images attach
You must be registered for see images attach
At this point I had starting doing all the over suspension work as well
New ball joints
New bushings in the lower control arms
New upper control arms and new rear upper control arm all from moog
I also started looking into a small lift for it and went with the rusty off-road strut spacer and poly block
You must be registered for see images attach
You must be registered for see images attach
It went in great but about after a week or so I had this annoying squeaking in the front which I originally thought was the coil spring rubbing on the frame and I had just got the new upper control arms so I didn’t want to go buy jba ones
So I decided to take it all apart again
And this is what I found
You must be registered for see images attach
You must be registered for see images attach
The washer from the strut assembly was slightly rubbing onto the lift spacer….. what I get for being cheap
But I took a grinder to the washer and solved my problem.
So at this point I had fixed all the oil leaks, done all my maintenance I was ready for do other little mods and get some new tires for the lift
You must be registered for see images attach
You must be registered for see images attach
You must be registered for see images attach
Installed a new steering wheel, xtrons android head unit (I didn’t want to change the OEM look)
At this point the flaws of the worn engine and trans were starting to show themselves I had an oil consumption issue. No leaks, new pcv valve and every 1500 miles was down a quart of oil
And I had to start topping off the coolant every month.
No overheating, i had already done dealt with a garden hose effect with the cooling system
Heater core was first then the radiator and coolant hoses with a new thermostat, then the water pump started leaking. So I knew I was at the point of cut my losses and get rid of it or ride it out as long as it last and fix it. We decided we liked it and to ride it out want fix it.
So we kept nursing it along and the trans started to develop a noise that i can only describe as a mosquito buzz.
I didn’t a bunch of reading and what I ended up doing was removing the cooler lines bypassing the cooler (just for the test) and the noise went away..